SUPER THERMAL POWER AT SINGRAULI, UP
CLIENT : National Thermal Power Corporation Ltd.
CONTRACTOR : CICO
Work Performed : October, 1985
SUBTERRANEAN
SOIL STABILISATION BY GROUTING OF TURBINE GENERATOR FOUNDATION
The Super Thermal Power
Corporation at U.P. has condenser unit adjoining the Turbine Generator (TG). The TG has a
massive foundation approximately 20m x 20m in plan and the level of the bottom of the TG
foundation is 9 m below the ground level. The adjoining condenser unit is about 20m x 5m
in plan dimension and the foundation is 12 m below the ground level.
After the TG foundation was completed, excavation
for the condenser unit was started. During the excavation, when the level reached was
about 12 m below the ground level, sand blow occurred from below the TG foundation,
leaving some gaping space below the foundation. Due to the movement of sand from the TG
foundation bottom, the authorities required rectification measures to ensure contact
between the bottom of the TG foundation concrete and the soil beneath it.

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PLAN
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CICO group was informed about the problem by M/s
Simplex Concrete Piles India Ltd., the main contractors and requested to evolve a suitable
rectification measure for ensuring proper contact.
After carefully considering the various problems
associated with the site, a solution involving cement and lime grouting was detailed out.
The procedure consisted of driving 100 mm dia pipes 8 nos at 3 m spacing in the 1.5m wide
space between the TG foundation and the condenser unit . The grouting was made through 30
mm dia pipes which were inserted in the casting pipe and a high pressure seal was
introduced between the 30 mm dia and the casting pipe. The initial grouting was at a
pressure of 0.5 bar (Kg/cm2). In order to ease the flow of cement-lime grout,
alongwith suitable admixtures, dewatering systems was introduced on the other side of the
TG foundation. Eight grouting points were utilised for the soil grouting and only one
grouting was handled at a time. On refusal of grout intake the grouting pressure was
gradually increased to 4 Kg/cm2, the same was maintained for about 15 minutes before
terminating the grouting. The process of grouting was successfully completed in a week's
time. |